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This headlamp shell Is a copy of an LC 250 light unit, I copied
this because it is cheap and easy to obtain replacement glass and
rim. The mould was made from an old plastic LC[RD250] headlight.
I have made lights from scratch, these were made to take Landrover
sealed beams, which again are very cheap and no problem to get.
This first headlamp shell layed up in this mould was made from
200 gm/metre twill, each layer was 2 pieces. To eliminate the frayed
edge join, I layed the carbon up on a polythene sheet and when the
epoxy had gone tacky I trimmed the frayed edges. This was a very
messy job and there were little pieces of epoxy carbon every where.
I was disappointed when I pulled it from the mould, it was very
badly pinholed. Looking at the surface of the mould it was obvious
that when it had been vacuumed small bubbles in the epoxy had expanded,
when I removed the laminate from the mould the epoxy over the expanded
air bubbles had stayed in the mould leaving a large pinhole in the
laminate, this also left a lattice of extremely thin epoxy on the
mould surface.
This headlamp shell was made of 200gm plain weave carbon fibre.
Each layer is 3 pieces of carbon fabric, 3 pieces were used so that
it would be easy to lay the carbon in the mould. I didnt have to
worry about the frayed edges with plain weave, well not as much
as twill anyway.
There are 4 layers of carbon, so the shell is about 1mm thick
and there are another couple of layers around the mounting holes
and the bolt holes for fastening the rim in. The rim fastening is
by 2 bolts at 4 and 8 o'clock and a rib at 12 o'clock, so a lip
was added to the shell to hold the rim.
Graff SE epoxy was used, this gave a working time of about half
an hour. I mixed the epoxy in a vacuum, so it didn't have any air
in it.
The pieces of carbon were layed up on a polythene sheet, the resin
was brushed on and squeegeed with a rubber tube roller.
Removal from the mould was very difficult, I had managed to get the
first one out of the mould without damaging the mould. I was fairly
confident that the surface of this was going to be OK so I had made
it thicker so it was to stiff to distort and release. I was forced
to cut the mould in half. There are several light cuts on the surface
of the laminate, but they are insignificant. The moulding got stuck
because the release angles were not large enough, the first part that
did release was flexible enought to compensate for this.
I had problems with the first headlights I made, due to carbon being
conductive. The shell had been made the correct size for the light
units, when a replacement light unit was fitted the terminals touched
the shell. This wasn't noticed until my brother was coming home from
the pub, he couldn't understand why dip was brighter than main and
the bloke following could smell burning epoxy. The shell had burned
around the terminals, I reinfoced the area with several layers of
Kevlar around the terminals. |
Figure 1. The plug, prior to painting, this is a plastic H/lamp
shell with a few modifications, the yellowy coloured stuff is body
filler. All radii were increased, all draft angles were increased,
the height was increased to allow some waste and a flange was added
to stick the bagging material to.
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